,vacuum deep-cut, creation of vacuum, distillation yield ,"/> <p class="MsoNormal" align="left" style="text-align:left;"> <b>250</b><b>万<span>t/a</span>常减压蒸馏装置减压深拔改造<span></span></b>

石油化工设计 ›› 2021, Vol. 38 ›› Issue (3): 4-9.doi: 10.3969/j.issn.1005-8168.2021.03.002

• 设计技术 • 上一篇    下一篇

250t/a常减压蒸馏装置减压深拔改造

梁泽涛1,刘登峰1,王亦成2,姜洁1,徐  1   

  1. 1.中石油华东设计院有限公司,山东 青岛 2660712. 中国石油天然气股份有限公司玉门油田分公司炼油化工总厂,甘肃 酒泉 735200
  • 收稿日期:2020-08-14 出版日期:2021-08-25 发布日期:2021-08-09
  • 作者简介:梁泽涛,男,2008年毕业于中国石油大学(华东)化学工艺专业,硕士,主要从事炼油装置工艺设计工作,副高级高级工程师。电话:0532-80950762

Deep-cut Revamping of 2.5 Mt/a Atmospheric and Vacuum Distillation Unit

Liang Zetao1, Liu Dengfeng1, Wang Yicheng2, Jiang Jie1, Xu Biao1   

  1. 1. CNPC EastChina Design Institute Co., Ltd., Qingdao, Shandong, 266071;  2. PetroChina Yumen Oilfield Company, Jiuquan, Gansu, 735200
  • Received:2020-08-14 Online:2021-08-25 Published:2021-08-09

摘要:

2016年,玉门炼化总厂250万吨/年常减压蒸馏装置实施了减压深拔和换热网络优化改造,通过换热网络集成、优化,原油换热终温从260℃提高到310℃;通过对减压塔减压深拔改造,包括润滑油型改造为燃料型,抽真空系统改造,减压炉改造,减压转油线改造等,原油实沸点切割温度达到565℃,减压蜡油收率提高6.47个百分点,优化了催化裂化装置进料,减压渣油收率降低6.86个百分点,降低了延迟焦化装置负荷,提高了全厂经济效益。

关键词: 减压深拔, 抽真空, 拔出率

Abstract:

In 2016, deep-cut revamping and heat exchanger network optimization were carried out on the 2.5 Mt/a atmospheric and vacuum distillation unit in Yumen refinery. The inlet temperature of crude furnace was increased from 260℃ to 310℃ after the integration and optimization of heat exchanger network. Through the deep-cut revamping of vacuum tower including the transformation from lubricating oil type to fuel type, the vacuum ejector system, the vacuum furnace and the vacuum transfer line, the TBP cut point of crude reached 565℃, the yield of VGO was improved by 6.47%, thus optimizing the feed to FCC unit. The yield of VR was decreased by 6.86%, reducing the load of DCU and improving the economic benefit of the refinery.

Key words:  ')">

 , vacuum deep-cut, creation of vacuum, distillation yield