石油化工设计 ›› 2020, Vol. 37 ›› Issue (1): 36-39.doi: 10.3969/j.issn.1005-8168.2020.01.010

• 工艺优化 • 上一篇    下一篇

某中东油田中心处理站工艺优化初探

李雷波,王亚彪   

  1. 中国石化工程建设有限公司,北京 100101
  • 收稿日期:2019-09-11 接受日期:2019-09-11 出版日期:2020-04-23 发布日期:2020-04-23
  • 通讯作者: 李雷波,lileibo@sei.com.cn E-mail:lileibo@sei.com.cn
  • 作者简介:李雷波,男,1994年毕业于山东建筑大学工业与民用建筑专业,工学学士,工程师。现任国际业务部副主任,高级工程师。从事石油化工设备的设计工作,已发表论文2篇,电话:010-84878277,E-mail: lileibo@sei.com.cn

Preliminary Study on Process Optimization of CTEP

Li Leibo, Wang Yabiao   

  1. SINOPEC Engineering Incorporation, Beijing, 100101
  • Received:2019-09-11 Accepted:2019-09-11 Online:2020-04-23 Published:2020-04-23
  • Contact: Li Leibo, Wang Yabiao,lileibo@sei.com.cn E-mail:lileibo@sei.com.cn

摘要: 对中东某油田中心处理站的原油处理工艺流程和设备的优化,提高了终端油气处理能力。通过优化段塞流捕集器内部结构增强气相的稳定性,优化气体压缩工艺流程来优化设备设置,综合优化一、二期气体物料达到优化设备选型、节约投资的目的;通过优化总工艺流程,简化气体压缩流程,达到稳定生产、节约投资、降低运行费用的目的,实现节能增效。

关键词: 中心处理站, 流程, 优化 气液分离, 段塞流捕集

Abstract: The terminal oil and gas processing capacity of the CTEP in an oil field in the Middle East was improved by optimizing the crude oil processing process and equipment. The stability of gas phase was enhanced by optimizing the internal design of slug catcher, the equipment setting was optimized by optimizing the gas compression process, and the equipment selection was optimized and the investment was saved by optimizing the Phase I and Phase II gas materials. By optimizing the overall process flow and simplifying the gas compression process, the goals of steady production, investment saving and operating cost reduction were achieved, the energy was saved and the efficiency was enhanced

Key words: CTEP, process, optimization, gas-liquid, separation, slug trapping